Well in the famous words of Jerry Garcia... What a long, strange trip its been. I have to say this has not only been a learning experience but one to test my patience. Moving forward I was able to barrow a proper bore gauge and found all the cylinders within .001 of spec for .040 over. I ordered up another set of pistons since trying to get a single piston was going to take weeks but a set I was able to get the next day. Go figure. New rings and con rod bearing. I had the head checked out and my buddy and I did a valve job just to clean things up. I also decided to put head studs in, for that just in case feeling. This proved to be a smart move.
As I was getting the short block back together, I had originally noticed that the left rear corner head bolt hole in the block had this "ring" sticking up. No knowing enough about this series of engines, I figured it was some locating point for the head gasket. Well I was sure wrong about that. After finding the head gasket did not sit over this, I carefully ground this flush with the head. I proceeded to install the head and start the step torquing. Things were going well until I got to 75 ft/lbs. This spot felt "soft" and would not torque. Well crap! Pull the head off and sure enough that ring was back. Figured out it was an insert that was pulling out of the block from a previous repair. Pull what was left of it out and I have no idea what type this was originally but it wasn't the right type as it had already pulled out prior to my dis-assembly the first time. Now I have to fix and already "fixed" hole. This presented it's own challenge as there are only a few inserts designed to fix a fixed hole. I ended up using an E-Z LOC insert. For this I needed to drill and tap the hole, which doing free hand is a challenge. Drilled and tapped, I put the head stud in and tried to fit the head. It would not line up on the dowel pins. I checked the stud and found side to side I was dead on but fore and aft, I was 1* off! One freakin' degree. With a 4" stud, this equated to about 1/16" or so. Crap! Posting up on an Inliner engine forum, I asked if I could open that hole up in the head slightly. Everyone seemed to agree it was fine to do so with an adjustable reamer, I opened it up a little. Success!!! I was able to fit the head and continue to assemble the engine. Nice thing with the head studs is, the insert is only taking vertical torque loads and not dealing with rotational load of torquing it. This should help prevent it from pulling out. Lots of new stuff installed and painted up the engine.
This past Saturday by best friend and I got the engine installed back in the wagon. This took a little bit of work and if I had to do it again, I would remove the forward cross member in the engine bay. It was tight working past it and not hanging up on the trans dropping it all back in. We get it mounted up and the exhaust reconnected. We worked on redoing the engine compartment wiring and completely redid most of the dash wiring with my completely new gauge setup I had custom built by Speedhut. Gauges came out awesome and have a very factory look to them. I had gotten these the week before the engine went south and had I had them installed, I likely would have caught the problem before damage occurred. Oh well. With all the wiring (and fixing a bunch of hack wiring from before), Saturday ended up being a 12 1/2 hour day. It is not finished and I still have a lot of work to do before it will be running.
While I had the engine out, I decided to redo the engine compartment brake lines which led me to replacing the booster and master cylinder as the universal one didn't really fit right and performance of it was so so. I ordered up a Nova specific one but it didn't come in, in time. I still have a couple weeks or so of work but a least it's moving forward. That gets me up to day but I know, where's the pics? Here's what I have off my camera at the moment. Enjoy.
Light hone of the cylinders
New piston and rings
Cleaned up the head and reassembling it
Pistons installed
Old insert pulled out, what it looked like and the E-Z LOC replacement (none installed though)
New gauges (temp installed in the old bezel as I ordered a new replacement)